I am trying to track down the causes of my GN/RX-7 idling so poorly. Hoping to find a vacuum leak, I pulled off the EGR valve and controller. No leak, so I put a little Ultra Copper on the gasket and bolted the valve back down. Prior to reinstalling, I put my MityVac to use on the controller vacuum ports. Pumped it up to about 15 psi and had a tiny amount of leakdown, but wasn't bad. Valve diaphragm was fine. So, I put 'er back together. When I fired it back up, the idle was HORRIBLE! Pushed on the valve and it was open?! Unplugged the controller and the idle settled down (the EGR shut when I did this). So, did I ruin the controller somehow? Just to make sure (the original hoses are long gone): the bigger vacuum hose goes to the intake hard line and the smaller to the EGR valve, correct?
Thanks! Jay
Thanks! Jay