Was a hot day that day. By the time we got onto the open road to test, it got to that temp. We (father and I) have put this new combo together. Prior the new 67/66 billet turbo,85# 's, alky kit and XFI car only came out to cruise. This was the 5th test hit in the new combo trynig to sort it out. It started really rich netting 8.8 af with the target of 10.9af at 24-25 psi. Took Cals advice and deducted 15% up top and smoothing the rest...but then it popped. But looking at the log when it popped it never went lean. We were actually closer to the 10.9-10.8 af target after the adjustment inthe VE table. I was thinking maybe the knock showing down low was the culprit of the gasket going, but i wanted to verify it here. This car was bought assuming the engine was fresh and ready to go 10's. Now im wondering if we might have bought something that wasnt real to the specs we were told it had. Maybe not... Maybe being soo rich the 1st 4 runs at 8.8-8.9 af ate away at the head gasket and took it out this last log when it popped.? Im just wanting to verify it wasnt the tune...