Here's what I did....I adjusted my wategate because I was making too much boost for the gas I was using (89 octane). I was maxing out at around 17-18 lbs. I gave the rod several turns counter-clockwise. I let the car warm up (Idle) for a few minutes and got a 44 CODE.
I located the vaccum leak (it was a line coming from the charcoal canister). I pluged it back in and took it for a run to see how the boost was doing and it ran like crap and I think I only saw about 8 lbs of boost. I know I may have adjusted too many turns but, after fixing the major vaccum leak, the thing won't hardly idle in gear and at a stop sign.
I would assume that it was idling fine with the vaccum leak and by plugging the leak, I wasn't making enough idle. Any ideas of why the idle is so low or what to do to fix it?
I located the vaccum leak (it was a line coming from the charcoal canister). I pluged it back in and took it for a run to see how the boost was doing and it ran like crap and I think I only saw about 8 lbs of boost. I know I may have adjusted too many turns but, after fixing the major vaccum leak, the thing won't hardly idle in gear and at a stop sign.
I would assume that it was idling fine with the vaccum leak and by plugging the leak, I wasn't making enough idle. Any ideas of why the idle is so low or what to do to fix it?