I think I may have found my problem
between last night and this morning i changed out the old springs for kirban HDs ,new retainers and keepers and had it buttoned back up around 930 am ,it feels crisper and vacuum picked up 1hg and is rock steady , took it for a run around the block and still dint feel like the top end was pulling , so i pulled off the Kenn bell ram air filter housing and tried again with GTech comp and the hp is way down as well as torque (130 hp at 4350 and 210torq at 3200 ), just a bit better than i read before the spring swap but i didnt know if it was accurate since i just got the Gtech last week , i didnt make it back to the buick meet and spent the day going over every inch of the motor rechecking all wire connections and tying back everything that moved or could shake . with the KB cover off i can now hear the turbo whistle and just reving it up i could hear theres a problem at the top end like flutter , figuring i would swap the turbo i started by taking of the sheild , undoing the down pipe and then decided to check the converter
after seperating the pipe from the cat i was able to pull out the down the pipe , If any one has never seen a catalytic melt down Ive got some nice pics , the front portion of the honeycomb was shattered and loose and the section after that melted down with little left for an exhaust path
now i just need to gut the cat and put it back together and hopefully it will run like a GN should and i can move on to cranking ithe boost up and Ill be looking for new DP and a high flow cat (need one in NJ ).