Never meet your heroes! '86 Grand National

I have two days left to get this thing drivable again, and I still have no idea why the narrowband is claiming lean.

I went to check and clean the MAF just in case. I thought I was on to something.
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All that nasty stuff is the goo that's used to protect the circuit board ozzing out. Post clean test drive revealed a very stable and reactive measurment, but still running lean. I'll note this oozing MAF and plan to upgrade to an LT1 sensor but for now I don't think it's the problem at hand.

At this point I really don't have time to wait for 600 degree turbos to ccol down before removing the down pipe, so I was just as careful as I could be. I did accidentally graze the header though which was an odd sensation. it was cool to the touch. This ethanol may be doing it's job afterall.
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I measured the hole at 1/2" with my small drill set. I don't have a full index or anything larger than 1/2" so I had to Amazon Prime a 33/64" and 17/32" drill bits. I'm pretty confident that 33/64" will do but I'm not taking any chances on wasting another day. While I was at it, I ordered an O2 bung. I need to get my spare wideband into this car and figure out if the narrowband is lying to me. I think the header would be very hot if the pistons were trying to go into meltdown mode.
 
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