Go Back   TurboBuick.Com > Tech Arena > General Turbo Buick Tech
Register FAQ Members List Photo Gallery Mark Forums Read



Welcome to the TurboBuick.Com forums.

You are currently viewing our boards as a guest which gives you limited access to view most discussions and access our other features. By joining our free community you will have access to post topics, communicate privately with other members (PM), respond to polls, upload content and access many other special features. Registration is fast, simple and absolutely free so please, join our community today!

If you have any problems with the registration process or your account login, please contact contact us.
Reply
 
LinkBack Thread Tools Display Modes
  #1 (permalink)  
Old December 20th, 2003, 03:53 PM
USAF
 
Join Date: Sep 2003
Location: Doha, Qatar
Trader Rating: (0)
Posts: 102
What damage could I have done?

Finally fixed my adj waist gate actuator today and I was taking the car out for a spin to see where the boost was. As soon as I got in the throttle the car shoots to 20psi and the I hear a loud pop! The rpm's drop from 4k to 1k almost instantly and the car continues running farily well. As soon as i pull over I realized that I didn't put the vac line on the actuator when I put it back in. I was only about 3 blocks from the house so I limped it home. The car ran fine but had a terrible hesitation. I was watching the temp and oil pressure the whole way and everything was fine. After I got home I discovered the the up pipe had blown off. I got everything hooked back up and the car seem to run well. Coolant level is normal as is the oil. Did the up-pipe blowing off prevent any damage to the motor? The engine has 144k on it and has never been opened. I will be replacing the vavle springs and timing chain next weekend. Should I go again and do the headgaskets?
__________________
Jeff
88 GTA, Gunmetal, L98 with every mod you can think of
87 IROC LT1 6-speed project
www.team3rdgen.com
Digg this Post!Add Post to del.icio.usBookmark Post in TechnoratiFurl this Post!
Reply With Quote
  #2 (permalink)  
Old December 20th, 2003, 04:04 PM
Senior Member
 
Join Date: Sep 2003
Location: Bucyrus, Ohio
Trader Rating: (0)
Posts: 311
It's O.K., the "fuse" just blew. Really, that has probably happened to most of us at one time or another and I've personally not hurt one yet. They sure run like crap when the pipe blows off though, don't they?
__________________
'86 WH1(My Favorite) , '89 TTA1543, '87 Porsche 911 Turbo, '86 Saleen Mustang, 9 second "no nitrous" S-10 and alot of "unfinished projects".
Digg this Post!Add Post to del.icio.usBookmark Post in TechnoratiFurl this Post!
Reply With Quote
  #3 (permalink)  
Old December 20th, 2003, 06:51 PM
d0n_3d's Avatar
What's in YOUR wallet!?
 
Join Date: Jul 2001
Location: Oak Lawn, IL & Valparaiso, IN
Trader Rating: (4)
Posts: 3,877
one time i was running my car on the highway up to 130 mph and my up pipe blew off...that was my first time...i thought the motor had blown up...i pulled over and expected the worst...needless to say i had the BIGGEST sigh of relief and i even had a flat screw driver on me!
__________________

-Don
87 GN 11.07 @ 125 mph (old combo w/ PT67 DBB, GN1 heads, 120k mile stock shortblock, ended up splitting block )

Now running a 44k original mile stock longblock, stock turbo (for now), PTE FMIC, 60 lb inj, TT chip, TA Perf 3" DP, GNX style VDO dash, Vince Janis built 200-4R w/ 10" 3400 n-l stall (can you say NO turbo lag? LOL)

Words of experience: Going fast was nice, but when your car is down every single year because you broke something, it isn't fun anymore and unless money grows on trees at your house, you don't regret going back to stock, and being able to drive and enjoy your car again
Digg this Post!Add Post to del.icio.usBookmark Post in TechnoratiFurl this Post!
Reply With Quote
  #4 (permalink)  
Old December 20th, 2003, 07:38 PM
2QWIK4U's Avatar
Senior Member
 
Join Date: May 2001
Location: Lockhart SC
Trader Rating: (0)
Posts: 244
First time it happened to me I just knew my car was toast!!Pulled over and put it back on using a quarter and pocket knife as a screwdriver.Everything is probaly ok.Reattach and drive , that will tell you for sure.
__________________
87 GN bought new,TE-44 w/PTE .68 housing,orange stripe converter,ATR double pumpers,ATR 313a cam,1.77 1.55 SS valves,THDP, red stripes ,Kenne Bell Ram Air,Joe Lubrant chips,scanmaster,7.40's 1/8 mile
86 Regal dirttrack car with SBC
Digg this Post!Add Post to del.icio.usBookmark Post in TechnoratiFurl this Post!
Reply With Quote
  #5 (permalink)  
Old December 20th, 2003, 08:35 PM
UNGN's Avatar
Can't Re- Member
 
Join Date: May 2001
Location: Southlake, TX
Trader Rating: (0)
Posts: 8,125
Smile

Don't tell anybody, but when TTA89's up pipe blew off, he called a wrecker and had his car towed home.

True story.
Digg this Post!Add Post to del.icio.usBookmark Post in TechnoratiFurl this Post!
Reply With Quote
  #6 (permalink)  
Old December 22nd, 2003, 03:25 AM
GN ERGY's Avatar
Senior Member
 
Join Date: Aug 2002
Location: OHIO / ARIZONA
Trader Rating: (0)
Posts: 1,431
I was in Bowling Green, with Jeremy as passenger running the video camera and I got on it and all of a sudden BOOM and the GN lost all power. The look on my face thought I just blew a headgasket, but turned out to be a hose came off. Jeremy put it back on and we were on our way.
Tarey D.
Digg this Post!Add Post to del.icio.usBookmark Post in TechnoratiFurl this Post!
Reply With Quote
  #7 (permalink)  
Old December 23rd, 2003, 01:23 AM
Razor's Avatar
Forum tech Advisor
 
Join Date: Jul 2001
Location: Tampa,Fl
Trader Rating: (5)
Posts: 8,954
Quote:
Originally posted by UNGN
Don't tell anybody, but when TTA89's up pipe blew off, he called a wrecker and had his car towed home.

True story.
Ohh boy..talk bout some dirt

Buy the HD T-Bolt clamps, silicon hoses, and you wont pop them off anymore...If theyre tightned down correctly.

I test mine weekly at 27 PSI make sure they dont pop off..

__________________
89 TTA Stock appearing
10.550 at 132.22 1.539 60ft 3850 race weight w/driver
Always on 93 octane
www.alkycontrol.com
727-570-9999
Digg this Post!Add Post to del.icio.usBookmark Post in TechnoratiFurl this Post!
Reply With Quote
Reply



Thread Tools
Display Modes

Posting Rules
You may not post new threads
You may not post replies
You may not post attachments
You may not edit your posts

vB code is On
Smilies are On
[IMG] code is On
HTML code is Off
Trackbacks are On
Pingbacks are On
Refbacks are On


All times are GMT -5. The time now is 08:30 PM.

Powered by vBulletin Version 3.6.2
Copyright ©2000 - 2008, Jelsoft Enterprises Ltd.
Content Relevant URLs by vBSEO 3.1.0
One of the largest message boards on the web !