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Anybody? Anything.
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87 GN,Walboro 340 w/upgrade,RJC FMIC, PWR Plate and Controller,wiring upgrades, GT 6152 Turbo,55# injectors,Adj fuel reg.TCS 9x11 3600stall and shiftkit.GenII,Turbotweaks chips. Dual fans,DP,Body Braces fr/Gbodyparts.H&R pro kit,engine mounts.Kirbans Valve springs, etc.Razors Alchy,Marks Electric cutout, Ashtray switches,glove box gauges.etc etc. 40 000 km.All internally stock 12.19@111.94.1.97 60ft/changed plugs to 032 gap.last run of season 11.67@115.19 1.74 sixty. Times in 08 11.74@116.97 w/1.90 60'. Exhaust leak/ Tuning by OI!/Need Better Brake System and a Torque Converter!! THANKS TO ALL G BODY VENDER'S,SELLERS and BOARD MEMBERS ![]()
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that seems like an awfully low RPM to be having a valve float issue even with old stockers.
My Wife's car has the old 160k mile stockers on it still and it can make it up to 5200 or so before it just really lays down and snoozes. That's at 24PSI or so (more boost = sooner valve float)
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Steve the Pirate The artist formerly known as MJRWOOD 87T |
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Thanks. I'm running 25 lbs boost, It's not really laying down and dieing just missing and hesitating. I'll try lowering the boost. I have a stock rpm guage so I started out lower. Closer were it starts missing would be over 4500.
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87 GN,Walboro 340 w/upgrade,RJC FMIC, PWR Plate and Controller,wiring upgrades, GT 6152 Turbo,55# injectors,Adj fuel reg.TCS 9x11 3600stall and shiftkit.GenII,Turbotweaks chips. Dual fans,DP,Body Braces fr/Gbodyparts.H&R pro kit,engine mounts.Kirbans Valve springs, etc.Razors Alchy,Marks Electric cutout, Ashtray switches,glove box gauges.etc etc. 40 000 km.All internally stock 12.19@111.94.1.97 60ft/changed plugs to 032 gap.last run of season 11.67@115.19 1.74 sixty. Times in 08 11.74@116.97 w/1.90 60'. Exhaust leak/ Tuning by OI!/Need Better Brake System and a Torque Converter!! THANKS TO ALL G BODY VENDER'S,SELLERS and BOARD MEMBERS ![]()
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Power drop off and possibly what seems like the engine is breaking up.
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![]() 1987 Regal LC2, hot-wired, Walbro 255 lph fuel pump, blue top injectors, Accufab adjustable fuel pressure regulator, Turbo Tweak chip, GN110T cam, TE-44 turbo, Alkycontrol, 3 inch mandrel bent Dynomax exhaust, RJC power plate and RJC boost controller |
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It sounds to me like you need to check your ignition grounds and/or your ignition module is weak. My ignition module went bad and had similar problems that progressively got worse over the course of a week or two untill it was popping and running rough under any boost at all. New Delco module and it ran like new.
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.020" Diamond pistons, Ported heads (206I/196E cfm) comp. 212/212 cam, 9.1:1 compression. Turbonetics 66BB, Dutt. neck TTA intercooler. Razor's alcohol kit. Turbo tweak chip. |
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Thanks Guys.
I'll check the Module just to be on the safe side.
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87 GN,Walboro 340 w/upgrade,RJC FMIC, PWR Plate and Controller,wiring upgrades, GT 6152 Turbo,55# injectors,Adj fuel reg.TCS 9x11 3600stall and shiftkit.GenII,Turbotweaks chips. Dual fans,DP,Body Braces fr/Gbodyparts.H&R pro kit,engine mounts.Kirbans Valve springs, etc.Razors Alchy,Marks Electric cutout, Ashtray switches,glove box gauges.etc etc. 40 000 km.All internally stock 12.19@111.94.1.97 60ft/changed plugs to 032 gap.last run of season 11.67@115.19 1.74 sixty. Times in 08 11.74@116.97 w/1.90 60'. Exhaust leak/ Tuning by OI!/Need Better Brake System and a Torque Converter!! THANKS TO ALL G BODY VENDER'S,SELLERS and BOARD MEMBERS ![]()
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Thanks everyone for your help. Problem solved when I changed my valve springs. Some of them I could squeeze over half closed with one hand. She pulls very hard up top now, and will have it at the track this week with new and improved times. Provided I get my new rear seal to arrrrg SEAL. The car only has 25k on it but after 20 yrs they get weak obviously. It was a cheap upgrade and fix.
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87 GN,Walboro 340 w/upgrade,RJC FMIC, PWR Plate and Controller,wiring upgrades, GT 6152 Turbo,55# injectors,Adj fuel reg.TCS 9x11 3600stall and shiftkit.GenII,Turbotweaks chips. Dual fans,DP,Body Braces fr/Gbodyparts.H&R pro kit,engine mounts.Kirbans Valve springs, etc.Razors Alchy,Marks Electric cutout, Ashtray switches,glove box gauges.etc etc. 40 000 km.All internally stock 12.19@111.94.1.97 60ft/changed plugs to 032 gap.last run of season 11.67@115.19 1.74 sixty. Times in 08 11.74@116.97 w/1.90 60'. Exhaust leak/ Tuning by OI!/Need Better Brake System and a Torque Converter!! THANKS TO ALL G BODY VENDER'S,SELLERS and BOARD MEMBERS ![]()
Last edited by waddell87 : June 3rd, 2008 at 04:32 AM. |
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Wow, never have I heard of a valve spring that could be squeezed with one hand. They must have been very weak.
If I may ask did you remove your heads to change the springs? Or did you bring the piston to TDC and fill with compressed air to keep the valve up while using a valve spring removal tool?
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![]() 1987 Regal LC2, hot-wired, Walbro 255 lph fuel pump, blue top injectors, Accufab adjustable fuel pressure regulator, Turbo Tweak chip, GN110T cam, TE-44 turbo, Alkycontrol, 3 inch mandrel bent Dynomax exhaust, RJC power plate and RJC boost controller |
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Quote:
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Jim '71 GS Buick 464/TH350 10 bolt 3:73 Bench seat/column shift 11.33@121 1.64 60' 87 T-Type Ltd (No mods) |
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Quote:
Just remove valve covers. spark plugs and use hose from a compression tester kit. Plug in air and away you go. I ordered Kirbans Valve springs and remover tool. Nice price.68 bucks. We did have to modify the tool to work. It was solid around so you couldn't press down on the spring to remove the keeper. easy fix though, just waste of time because I didn't notice it right away. By the way make sure you have a spare rocker arm on hand or a piece of pipe the same size with holes drilled in it to fit the tool on, to attach too head so you can compress the spring with the tool. Basically their tool is an old rocker with a S pipe. I used another pipe because i didn't want to remove my rockers in case I broke the little plastic tabs that hold rocker in place. S piece is used for leverage. Passenger side is...You guessed it... PITA, last one anyways. Small hands would help.Don't push too HARD on spring or you release the air and the you WILL have to remove your head to get the valve out. Hope I made some sense and it helps you.. Gnttpe.org has a piece written on it too. Big difference tho..Holy Cow. I can't wait to see what mph i'm getting from the 1/8 to the 1/4. I was getting 18- 20mph gain before. hopefully 25+ now.
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87 GN,Walboro 340 w/upgrade,RJC FMIC, PWR Plate and Controller,wiring upgrades, GT 6152 Turbo,55# injectors,Adj fuel reg.TCS 9x11 3600stall and shiftkit.GenII,Turbotweaks chips. Dual fans,DP,Body Braces fr/Gbodyparts.H&R pro kit,engine mounts.Kirbans Valve springs, etc.Razors Alchy,Marks Electric cutout, Ashtray switches,glove box gauges.etc etc. 40 000 km.All internally stock 12.19@111.94.1.97 60ft/changed plugs to 032 gap.last run of season 11.67@115.19 1.74 sixty. Times in 08 11.74@116.97 w/1.90 60'. Exhaust leak/ Tuning by OI!/Need Better Brake System and a Torque Converter!! THANKS TO ALL G BODY VENDER'S,SELLERS and BOARD MEMBERS ![]()
Last edited by waddell87 : June 4th, 2008 at 01:26 AM. |
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Ive been meaning to do mine in my GN. Granted it still pulls good, but with 100,000 on the motor; I'd rather spend $200 to get the job done the a few thousand for a new motor. I did them on my old WH-1 when it had 135K on it and I gained 2/10ths just from those alone. No other mods. Really woke the car up.
I need to do the springs and a few other small things before I hit the track again.
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Scott Jackson aka "ScoJack" MAGNA Member & Methanol Dealer... '86 GN... Mild mods & Razors PAC with Limited Bronsonian Modification. 11.980@111.51 w/ 1.64 60' still with trans issues, but its got 1st now... STOCK TURBO, IC, CAM, CONVERTOR... THROUGH THE EXHAUST!!! |
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