Go Back   TurboBuick.Com > Tech Arena > Engine Tech
Register FAQ Members List Photo Gallery Mark Forums Read



Welcome to the TurboBuick.Com forums.

You are currently viewing our boards as a guest which gives you limited access to view most discussions and access our other features. By joining our free community you will have access to post topics, communicate privately with other members (PM), respond to polls, upload content and access many other special features. Registration is fast, simple and absolutely free so please, join our community today!

If you have any problems with the registration process or your account login, please contact contact us.
Reply
 
LinkBack Thread Tools Display Modes
  #1 (permalink)  
Old May 13th, 2008, 05:28 PM
waddell87's Avatar
Grasshopper
 
Join Date: Apr 2006
Location: Edmonton,Alberta
Trader Rating: (0)
Posts: 349
Valve Float

Hi Guy's
Does any one have any tell tale signs of floating the valves.
Everything was working good before I changed my DP from an older 21/2 meese to a 3 inch and electric cut out. My btm end power is good all my scanmaster readings are fine. butt, at over 3500-4000 rpm or 3/4 to WOT its sounds terrible especially with the dump open!
It's missing and stumbling best I can describe it. I'm guessing valve float because everything was good before. My valve springs are still stock.
Thanks for any Input all is welcome. btw plugs are good, gapped to .032 and wires and pack are good. I did a search but no definite answers.
__________________
87 GN,Walboro 340 w/upgrade,RJC FMIC, PWR Plate and Controller,wiring upgrades, GT 6152 Turbo,55# injectors,Adj fuel reg.TCS 9x11 3600stall and shiftkit.GenII,Turbotweaks chips. Dual fans,DP,Body Braces fr/Gbodyparts.H&R pro kit,engine mounts.Kirbans Valve springs, etc.Razors Alchy,Marks Electric cutout, Ashtray switches,glove box gauges.etc etc. 40 000 km.All internally stock 12.19@111.94.1.97 60ft/changed plugs to 032 gap.last run of season 11.67@115.19 1.74 sixty. Times in 0811.74@116.97 w/1.90 60'. Exhaust leak/ Tuning by OI!/Need Better Brake System and a Torque Converter!!

THANKS TO ALL G BODY VENDER'S,SELLERS and BOARD MEMBERS
Digg this Post!Add Post to del.icio.usBookmark Post in TechnoratiFurl this Post!
Reply With Quote
  #2 (permalink)  
Old May 13th, 2008, 08:39 PM
waddell87's Avatar
Grasshopper
 
Join Date: Apr 2006
Location: Edmonton,Alberta
Trader Rating: (0)
Posts: 349
Anybody? Anything.
__________________
87 GN,Walboro 340 w/upgrade,RJC FMIC, PWR Plate and Controller,wiring upgrades, GT 6152 Turbo,55# injectors,Adj fuel reg.TCS 9x11 3600stall and shiftkit.GenII,Turbotweaks chips. Dual fans,DP,Body Braces fr/Gbodyparts.H&R pro kit,engine mounts.Kirbans Valve springs, etc.Razors Alchy,Marks Electric cutout, Ashtray switches,glove box gauges.etc etc. 40 000 km.All internally stock 12.19@111.94.1.97 60ft/changed plugs to 032 gap.last run of season 11.67@115.19 1.74 sixty. Times in 0811.74@116.97 w/1.90 60'. Exhaust leak/ Tuning by OI!/Need Better Brake System and a Torque Converter!!

THANKS TO ALL G BODY VENDER'S,SELLERS and BOARD MEMBERS
Digg this Post!Add Post to del.icio.usBookmark Post in TechnoratiFurl this Post!
Reply With Quote
  #3 (permalink)  
Old May 13th, 2008, 08:50 PM
BEATAV8's Avatar
The Engine Whisperer
 
Join Date: Feb 2002
Location: Lake in the Hills, IL
Trader Rating: (0)
Posts: 1,042
that seems like an awfully low RPM to be having a valve float issue even with old stockers.

My Wife's car has the old 160k mile stockers on it still and it can make it up to 5200 or so before it just really lays down and snoozes. That's at 24PSI or so (more boost = sooner valve float)
__________________
Steve the Pirate
The artist formerly known as MJRWOOD
87T
Digg this Post!Add Post to del.icio.usBookmark Post in TechnoratiFurl this Post!
Reply With Quote
  #4 (permalink)  
Old May 13th, 2008, 09:37 PM
waddell87's Avatar
Grasshopper
 
Join Date: Apr 2006
Location: Edmonton,Alberta
Trader Rating: (0)
Posts: 349
Thanks. I'm running 25 lbs boost, It's not really laying down and dieing just missing and hesitating. I'll try lowering the boost. I have a stock rpm guage so I started out lower. Closer were it starts missing would be over 4500.
__________________
87 GN,Walboro 340 w/upgrade,RJC FMIC, PWR Plate and Controller,wiring upgrades, GT 6152 Turbo,55# injectors,Adj fuel reg.TCS 9x11 3600stall and shiftkit.GenII,Turbotweaks chips. Dual fans,DP,Body Braces fr/Gbodyparts.H&R pro kit,engine mounts.Kirbans Valve springs, etc.Razors Alchy,Marks Electric cutout, Ashtray switches,glove box gauges.etc etc. 40 000 km.All internally stock 12.19@111.94.1.97 60ft/changed plugs to 032 gap.last run of season 11.67@115.19 1.74 sixty. Times in 0811.74@116.97 w/1.90 60'. Exhaust leak/ Tuning by OI!/Need Better Brake System and a Torque Converter!!

THANKS TO ALL G BODY VENDER'S,SELLERS and BOARD MEMBERS
Digg this Post!Add Post to del.icio.usBookmark Post in TechnoratiFurl this Post!
Reply With Quote
  #5 (permalink)  
Old May 13th, 2008, 10:02 PM
87Regal3.8SFI's Avatar
V6 on steroids
 
Join Date: Jan 2007
Location: Missouri
Trader Rating: (1)
Posts: 1,850
Quote:
Originally Posted by waddell87 View Post
Hi Guy's
Does any one have any tell tale signs of floating the valves.
Power drop off and possibly what seems like the engine is breaking up.
__________________

1987 Regal LC2, hot-wired, Walbro 255 lph fuel pump, blue top injectors, Accufab adjustable fuel pressure regulator, Turbo Tweak chip, GN110T cam, TE-44 turbo, Alkycontrol, 3 inch mandrel bent Dynomax exhaust, RJC power plate and RJC boost controller
Digg this Post!Add Post to del.icio.usBookmark Post in TechnoratiFurl this Post!
Reply With Quote
  #6 (permalink)  
Old May 15th, 2008, 03:37 PM
Senior Member
 
Join Date: Feb 2006
Trader Rating: (0)
Posts: 247
It sounds to me like you need to check your ignition grounds and/or your ignition module is weak. My ignition module went bad and had similar problems that progressively got worse over the course of a week or two untill it was popping and running rough under any boost at all. New Delco module and it ran like new.
__________________
.020" Diamond pistons, Ported heads (206I/196E cfm) comp. 212/212 cam, 9.1:1 compression. Turbonetics 66BB, Dutt. neck TTA intercooler. Razor's alcohol kit. Turbo tweak chip.
Digg this Post!Add Post to del.icio.usBookmark Post in TechnoratiFurl this Post!
Reply With Quote
  #7 (permalink)  
Old May 16th, 2008, 01:37 AM
waddell87's Avatar
Grasshopper
 
Join Date: Apr 2006
Location: Edmonton,Alberta
Trader Rating: (0)
Posts: 349
Thanks Guys.

I'll check the Module just to be on the safe side.
__________________
87 GN,Walboro 340 w/upgrade,RJC FMIC, PWR Plate and Controller,wiring upgrades, GT 6152 Turbo,55# injectors,Adj fuel reg.TCS 9x11 3600stall and shiftkit.GenII,Turbotweaks chips. Dual fans,DP,Body Braces fr/Gbodyparts.H&R pro kit,engine mounts.Kirbans Valve springs, etc.Razors Alchy,Marks Electric cutout, Ashtray switches,glove box gauges.etc etc. 40 000 km.All internally stock 12.19@111.94.1.97 60ft/changed plugs to 032 gap.last run of season 11.67@115.19 1.74 sixty. Times in 0811.74@116.97 w/1.90 60'. Exhaust leak/ Tuning by OI!/Need Better Brake System and a Torque Converter!!

THANKS TO ALL G BODY VENDER'S,SELLERS and BOARD MEMBERS
Digg this Post!Add Post to del.icio.usBookmark Post in TechnoratiFurl this Post!
Reply With Quote
  #8 (permalink)  
Old June 3rd, 2008, 03:34 AM
waddell87's Avatar
Grasshopper
 
Join Date: Apr 2006
Location: Edmonton,Alberta
Trader Rating: (0)
Posts: 349
Thanks everyone for your help. Problem solved when I changed my valve springs. Some of them I could squeeze over half closed with one hand. She pulls very hard up top now, and will have it at the track this week with new and improved times. Provided I get my new rear seal to arrrrg SEAL. The car only has 25k on it but after 20 yrs they get weak obviously. It was a cheap upgrade and fix.
__________________
87 GN,Walboro 340 w/upgrade,RJC FMIC, PWR Plate and Controller,wiring upgrades, GT 6152 Turbo,55# injectors,Adj fuel reg.TCS 9x11 3600stall and shiftkit.GenII,Turbotweaks chips. Dual fans,DP,Body Braces fr/Gbodyparts.H&R pro kit,engine mounts.Kirbans Valve springs, etc.Razors Alchy,Marks Electric cutout, Ashtray switches,glove box gauges.etc etc. 40 000 km.All internally stock 12.19@111.94.1.97 60ft/changed plugs to 032 gap.last run of season 11.67@115.19 1.74 sixty. Times in 0811.74@116.97 w/1.90 60'. Exhaust leak/ Tuning by OI!/Need Better Brake System and a Torque Converter!!

THANKS TO ALL G BODY VENDER'S,SELLERS and BOARD MEMBERS

Last edited by waddell87 : June 3rd, 2008 at 04:32 AM.
Digg this Post!Add Post to del.icio.usBookmark Post in TechnoratiFurl this Post!
Reply With Quote
  #9 (permalink)  
Old June 3rd, 2008, 04:34 PM
87Regal3.8SFI's Avatar
V6 on steroids
 
Join Date: Jan 2007
Location: Missouri
Trader Rating: (1)
Posts: 1,850
Wow, never have I heard of a valve spring that could be squeezed with one hand. They must have been very weak.

If I may ask did you remove your heads to change the springs? Or did you bring the piston to TDC and fill with compressed air to keep the valve up while using a valve spring removal tool?
__________________

1987 Regal LC2, hot-wired, Walbro 255 lph fuel pump, blue top injectors, Accufab adjustable fuel pressure regulator, Turbo Tweak chip, GN110T cam, TE-44 turbo, Alkycontrol, 3 inch mandrel bent Dynomax exhaust, RJC power plate and RJC boost controller
Digg this Post!Add Post to del.icio.usBookmark Post in TechnoratiFurl this Post!
Reply With Quote
  #10 (permalink)  
Old June 3rd, 2008, 05:55 PM
gusszgs's Avatar
Member
 
Join Date: Dec 2007
Location: Barrie,Ont
Trader Rating: (1)
Posts: 40
Quote:
Originally Posted by 87Regal3.8SFI View Post
Wow, never have I heard of a valve spring that could be squeezed with one hand. They must have been very weak.

If I may ask did you remove your heads to change the springs? Or did you bring the piston to TDC and fill with compressed air to keep the valve up while using a valve spring removal tool?
Ya, kinda curious myself on how hard it is to change out the springs. And what did you replace them with, brand wise.
__________________
Jim
'71 GS Buick
464/TH350
10 bolt 3:73
Bench seat/column shift
11.33@121 1.64 60'

87 T-Type Ltd (No mods)
Digg this Post!Add Post to del.icio.usBookmark Post in TechnoratiFurl this Post!
Reply With Quote
  #11 (permalink)  
Old June 4th, 2008, 01:14 AM
waddell87's Avatar
Grasshopper
 
Join Date: Apr 2006
Location: Edmonton,Alberta
Trader Rating: (0)
Posts: 349
Quote:
Originally Posted by 87Regal3.8SFI View Post
Wow, never have I heard of a valve spring that could be squeezed with one hand. They must have been very weak.

If I may ask did you remove your heads to change the springs? Or did you bring the piston to TDC and fill with compressed air to keep the valve up while using a valve spring removal tool?
Guess I'm 2 up on you then. Plus i've worked rigs for 21 yrs so probably have bit more hand strength than the avg. joe. but yes, they, not all, were quite weak.

Just remove valve covers. spark plugs and use hose from a compression tester kit. Plug in air and away you go.
I ordered Kirbans Valve springs and remover tool. Nice price.68 bucks. We did have to modify the tool to work. It was solid around so you couldn't press down on the spring to remove the keeper. easy fix though, just waste of time because I didn't notice it right away. By the way make sure you have a spare rocker arm on hand or a piece of pipe the same size with holes drilled in it to fit the tool on, to attach too head so you can compress the spring with the tool. Basically their tool is an old rocker with a S pipe. I used another pipe because i didn't want to remove my rockers in case I broke the little plastic tabs that hold rocker in place. S piece is used for leverage. Passenger side is...You guessed it... PITA, last one anyways. Small hands would help.Don't push too HARD on spring or you release the air and the you WILL have to remove your head to get the valve out. Hope I made some sense and it helps you.. Gnttpe.org has a piece written on it too.

Big difference tho..Holy Cow. I can't wait to see what mph i'm getting from the 1/8 to the 1/4. I was getting 18- 20mph gain before. hopefully 25+ now.
__________________
87 GN,Walboro 340 w/upgrade,RJC FMIC, PWR Plate and Controller,wiring upgrades, GT 6152 Turbo,55# injectors,Adj fuel reg.TCS 9x11 3600stall and shiftkit.GenII,Turbotweaks chips. Dual fans,DP,Body Braces fr/Gbodyparts.H&R pro kit,engine mounts.Kirbans Valve springs, etc.Razors Alchy,Marks Electric cutout, Ashtray switches,glove box gauges.etc etc. 40 000 km.All internally stock 12.19@111.94.1.97 60ft/changed plugs to 032 gap.last run of season 11.67@115.19 1.74 sixty. Times in 0811.74@116.97 w/1.90 60'. Exhaust leak/ Tuning by OI!/Need Better Brake System and a Torque Converter!!

THANKS TO ALL G BODY VENDER'S,SELLERS and BOARD MEMBERS

Last edited by waddell87 : June 4th, 2008 at 01:26 AM.
Digg this Post!Add Post to del.icio.usBookmark Post in TechnoratiFurl this Post!
Reply With Quote
  #12 (permalink)  
Old June 5th, 2008, 09:08 AM
Livin' Like A Refugee
 
Join Date: May 2001
Location: Bear, DE USA
Trader Rating: (1)
Posts: 315
Ive been meaning to do mine in my GN. Granted it still pulls good, but with 100,000 on the motor; I'd rather spend $200 to get the job done the a few thousand for a new motor. I did them on my old WH-1 when it had 135K on it and I gained 2/10ths just from those alone. No other mods. Really woke the car up.

I need to do the springs and a few other small things before I hit the track again.
__________________
Scott Jackson aka "ScoJack"
MAGNA Member & Methanol Dealer...

'86 GN... Mild mods & Razors PAC with Limited Bronsonian Modification. 11.980@111.51 w/ 1.64 60' still with trans issues, but its got 1st now...

STOCK TURBO, IC, CAM, CONVERTOR... THROUGH THE EXHAUST!!!
Digg this Post!Add Post to del.icio.usBookmark Post in TechnoratiFurl this Post!
Reply With Quote
Reply



Thread Tools
Display Modes

Posting Rules
You may not post new threads
You may not post replies
You may not post attachments
You may not edit your posts

vB code is On
Smilies are On
[IMG] code is On
HTML code is Off
Trackbacks are On
Pingbacks are On
Refbacks are On

Similar Threads
Thread Thread Starter Forum Replies Last Post
valve float??? or something else? TURBOELKY General Turbo Buick Tech 9 November 16th, 2007 11:02 AM
valve float...whats it sound like? 87NAT General Turbo Buick Tech 10 November 2nd, 2007 03:19 PM
ignition/valve float? snzuloz General Turbo Buick Tech 1 July 10th, 2006 04:54 AM
valve float buickpower General Turbo Buick Tech 13 October 8th, 2005 08:51 PM
valve float? shmed General Turbo Buick Tech 2 September 23rd, 2004 11:34 AM


All times are GMT -5. The time now is 07:11 AM.

Powered by vBulletin Version 3.6.2
Copyright ©2000 - 2008, Jelsoft Enterprises Ltd.
Content Relevant URLs by vBSEO 3.1.0
One of the largest message boards on the web !