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Old September 21st, 2007, 01:05 PM
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86 TR 86 TR is offline
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Join Date: Mar 2007
Location: New Glarus, WI
Trader Rating: (4)
Posts: 668
Well not today. But went racing last saturday. The car felt good. Runs were in the mid-low 11's felt the car surge and then the temp gauge was climbing. Look what I found!











Ive never blown both headgaskets at once before!! Talk about doing the job right! The car never had any detonation during any of the runs so I know that I hurt them from before when I got a little crazy on the street with not enough octane, and letting a buddy drive it that doesn't know how to drive!!

Anyways pulled the engine sunday morning, dissassembled everything to find this. Plus the oil pan had about 2 gallons of antifreeze mixed in with it. Not too good of a weekend. Now its time to go all out!!!! The block is at the machine shop already getting line bored with new billet caps, steel crank, and new pistons.

Maybe this weekend will be better. I ordered some ported heads, intake, roller cam already.
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2000 Ford Crown Vic. daily driven beater, 1986 Buick Regal T-type Dk. Blue Metallic, tan leather interior, column shift, TE60, ported irons, intake, 212-206 hydraulic roller, HS 1.55 roller rockers, Precision Stock Loc. intercooler, RJC valve cover spacers, 60lb.motrons, red's 93 street chip, trans. built by Jimmy's Transmissions, orange stripe converter. No new track times with new combo. Old combo went 11.30's @ 119mph.

Last edited by 86 TR : September 21st, 2007 at 01:15 PM.
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